My
4th Morgan Invasion
By,
Bob Horan
April
2007
With
the preparations behind me, I hit the road on Tuesday the 18th of April about
noon. I always expect trouble when I
am one the road and this trip was no different. It was a windy day and driving the 8 miles to Interstate 75 was
the first lesson in what can happen. I
could not get my truck to go faster than 40 miles per hour in high gear going
against the wind. I had thoughts that I
might have to turn around and check to see if all 8 cylinders were firing. When I hit Interstate 75 and turned South,
no problem, up to 60 mph and I was cruising but I noticed a little
vibration. Must be the road. I made it into Florida and the vibration was
still there, so I crawled under the truck and checked the drive shafts. I could not see or feel a problem. After a little rest, I drove on and arrived
at the Davis Island Public Boat Ramp about 6AM., with the high tide expected
about 14:00. I took my time getting
the boat ready and at 14:00 I recruited a couple of gentlemen to help me launch
because by then there was a 15mph cross wind on the ramp. After parking my truck and trailer at
Davis Island Yacht Club, I sailed away from the dock at about 15:00. Life was good and I was sailing again. Checking the chart, I decided to sail to a
small spoil island about 5 miles out.
By 17:00 I was sailing into a protected cove on the back side of the
island, with one other boat anchored.
I set out a couple of anchors and dinghyed in to shore for a walk &
swim. My boat was joined by 33 ft
Ericson sailboat as I swam a few strokes in the cool water. The night was quiet, but Wednesday promised
to have 15mph winds.
I
got up early and by 9Am I was pulling up my anchors and sailing away from my
deserted island shelter. The wind was
coming from the Southwest and I wanted to sail to the Southwest. I tacked upwind toward my destination,
Egmont Key located about 8 miles past the Tampa Bay Bridge. Around noon the wind dipped to about
7mph. I shook out the reefs in the jib
and main and started making pretty good time.
It was not 45 minutes later that the wind was back up past 15mph and I
was setting my new tiller pilot to steer the boat while I reefed again. With the reefs in I beat upwind again until
2:45PM. I was still 4-5 miles away from
the bridge and there was no way I could make Egmont Key before dark. I looked at the chart for protected
anchorages and decided I would buzz by St Pete, then turn down wind and sail
back to the spoil island I had anchored behind the night before. It took 2 hours to sail back to the spoil
island after leaving St. Pete. 11 miles
in 2 hours. At times I thought the
dinghy would get pooped but it skidded ahead of the waves just in time. By 5:15, I was anchored with all my anchors
out and only 50ft away from the beach.
The 20mph wind had shifted and I was only being protected from the waves
now. A small sand bar on the South
side of the island was my only protection.
The other boats at anchor were further out and were rocking and
rolling.
The next morning I found the wind had
done a 180 on me and the island was again barely blocking the wind and the
waves. I decided after checking the
wind, that I would just stay there for the day and wander on the island, and
maybe do some reading. I wanted to
check out the awning I had made and today was the day. It worked well except that the PVC pipe I
used would eventually be permanently bent and would not provide any tension. I would have to work on that. Maybe some fiberglass rods inside of the PVC
pipe. About noon, I noticed a Macgregor
22 motoring past and dropping anchor near the shore. I decided to take the dinghy in and found the owner up the
island some picking up trash. His name
was Bruce Avery and no, cleaning up the island was not his Job. He had worked for the Dept Of Natural
Resources in Michigan and after retiring had moved to Apollo Beach, FL. and a
few years back had decided the island was getting a lot of trash on it and
started coming out to pick up the trash since no one else was doing it. We exchanged backgrounds and I asked if he
had a spare trash bag that I could use to help him. He said he was leaving soon and I told him I could have a bag
full in 20 minutes and would meet him at his boat. 20 minutes later I struggled out of the trees to the beach
carrying a full bag of trash to his MacGregor. He was waiting and surprised I had returned with a full
bag. We talked a little more and as he
prepared to pull up his anchor and motor back home, he invited me to come down
from Georgia anytime to spend time at the island and to help him pick up trash
on it. With the awning up the boat was
a great place to relax in the afternoon, reading and watching the many visitors
to the island. By 7PM there were only
a couple of people on the island and I took the dinghy ashore to watch the
sunset on the opposite side of the island.
I had a quiet night because this time the island was blocking both the
wind and the waves.
Friday morning was quiet with barely a
whisper of wind as I pulled up my anchors and prepared to sail to Davis Island
Yacht Club (DIYC) for the Morgan Invasion.
I sailed leisurely along and by 3PM I took down the sails and motored
into the channel to the seaplane basin.
As I passed by the Yacht Club, I smelled something hot and after
checking the motor, I found I had no cooling water. I would have to work on the motor, probably a water pump. As the evening came I asked around and found
not much in the way of a Honda Outboard dealer that might have the parts. Finally
I found one near Brandon and would try to get a water pump kit from them
in the morning. After dinner, Charley
Morgan gave a presentation about his early days of sailing Tampa Bay, his
adventures in the sail making business and then yacht building &
racing, leading into Morgan Yacht
Corp. Linda and Chris (my crew for the
race on Saturday) arrived about the time Charley was finishing up and we
developed a plan for the next day.
The first thing Saturday, we had to
replace a lower shroud on the starboard side because of a long crack in the
crimp of the original, so Chris winched me up the mast so I could connect the
new one. With the lower shroud
replaced, we were off searching for a water pump kit and breakfast. We arrived back at the Yacht Club just as
the gun had gone off for the skippers meeting. As we were coming away from the meeting, Tim Horsman
arrived. He would be my third
crewmember for the race. He owns
"Blue Cloud" a M24 that he sails and races out of St. Pete. We had to get a tow out to the race and
"Dungle Jums" a Morgan 22, (hull # 1) volunteered to do that. Our timing for the start was off by a
minute so we had a late start and lost some time on the first leg. The second leg, was a downwind and Tim
suggested we take down the 100% jib and put up the 120%. Without loosing any time against the boats
around us, we put up the 120% and immediately could feel the difference. We sailed the course making a few errors
including leaving the centerboard up on one upwind leg, and bumping one
buoy. At one point, Tim stepped below
to find the carpet wet. I had
forgotten to shut off the sink freshwater feed and because of the heel of the
boat, the water had run out of the bow water tank and into the sink, running out
on the counter and into the bilge.
Running the bilge pump for a couple of minutes was enough to get a lot
of the water out. For the last three
legs of the race the wind was blowing over twenty. Watching the GPS to stay on course on one leg, we watched the boat
speed go to over 7kts for most of that leg.
As we came onto the last leg of the race, we decided to reef the
main. With that done we made a couple
of tacks to line us up with the finish line.
We could get fifth!! With a
wind shift we had to bear off some, and "Amanda" (another Morgan 24)
was coming in very fast. We had to make
one more short tack near the finish and as we straightened out to sail to the
finish line, "Amanda" came by
us and beat us to the finish line by 5 seconds. We got 6th place out of 8 in our class. We lost our whisker pole on our last tack,
so we turned around to see if we could find it. It was in the extended position and was about 14ft. long. It was easy to see. It was sticking straight up, 1 foot out of
the water, the other end was resting on the bottom. We sailed into DIYC and using the motor for just a short time we
made it back to the dock. Linda was
soaking wet and the rest of us were only half wet. Dinner and the racing awards followed. We all slept pretty good that night although my bunk was wet from
water that had leaked in from the seat hatches when we had heeled over so far
on the last couple of legs of the race.
The following morning Chris and I tried
to get the Honda apart enough to replace the water pump impeller. Not successful and by 10Am it was time for
Linda & Chris to head out. I
cleaned up the boat some, trying to get things dried out. In the afternoon, walking back from the
truck, I talked with George Russell, (Unplugged, Morgan 27) about his Honda 8
and in the process, he told me how to get my Honda apart and what to look for
to check out the whole cooling system.
With that knowledge, I knew I would have to spend quite a little money
to have a marina do the work or I could cancel the plans to sail in Charlotte
Harbor, do the Mug race, and just pack up the boat to go home to do the work at
the house. Either way, just replacing
the impeller would not be enough. I
opted to pull out on Monday when the boat ramp would be not very crowded and I
would drive home on Monday evening.
With an early start and a 10mph wind, I
sailed away from the DIYC dock with a reefed main only. I knew I would have to sail to the dock
with no motor and I did not want to have to manage too many sails at one time
since I would be going down wind to get to the dock. I managed to sail up to the dock and at the last minute stall
the boat to let it slide gently up to the dock. Just like I knew what I was doing. Loading the boat on the trailer took a little time but was
uneventful although I did have to wait for a couple of hours for the tide to
come up enough that I would be able float the boat onto the trailer. I spent the afternoon taking the mast down
and getting the boat ready for the drive home. I waited until after supper to crank up and start my drive thru
Tampa. By 7 PM. the roads were nearly
empty and driving North on I 275, I started feeling a vibration as I got above
50 Mph. By the time I merged onto I 75
I could tell that I had a serious problem with the drive train on the
truck. It was probably the universal
joint on the front of the read drive shaft this time. Last year it was the rear one that went out. By the time I got to Warner Robins, the
outside mirrors were a blur from the vibration. I had driven easy the whole time hoping that I would not have a
failure on the road. I arrived home
at 8AM safe and sound. By 9AM, I was
sliding under the truck beginning the process of replacing all the remaining
(original 1972) universal joints, including the one that had come so close to
breaking on the drive home. The
following day, I started on the Honda outboard and found a frozen thermostat
and a pump impeller that had no fins on it.
I ordered the parts from Plantation Marine in Eatonton and had the
outboard motor back together & running great 4 days later. I look forward to attending the Morgan
Invasion again next year.